Title: Boost leak or failed component? Post by: dokalanyi on January 06, 2017, 02:05:52 PM Hi All,
I'm getting WGDC of 100%. Car was running fine on same tune. It has cut off power at one point, but I failed to replicate even after hard driving. I've attached logs. Title: Re: Boost leak or failed component? Post by: dokalanyi on January 06, 2017, 02:12:05 PM Couldn't figure out how to modify attachments, here is the log when car was fine. Same tune.
Title: Re: Boost leak or failed component? Post by: nyet on January 06, 2017, 04:16:34 PM did fueling change?
if it were a boost leak, i'd expect the opposite lambda control action. Title: Re: Boost leak or failed component? Post by: nyet on January 06, 2017, 04:20:17 PM I'd say turbo failing or collapsing inlet, or some other restriction.
Title: Re: Boost leak or failed component? Post by: dokalanyi on January 06, 2017, 08:17:54 PM did fueling change? if it were a boost leak, i'd expect the opposite lambda control action. Fueling didn't change, and trims are -0.2% and -5.5%. I'll open her up today and inspect the turbo and hoses. There is also a very low pitch whistle when I accelerate (around 2k rpm). Title: Re: Boost leak or failed component? Post by: ktm733 on January 07, 2017, 09:48:54 AM Do you have a catalytic converter?
Title: Re: Boost leak or failed component? Post by: nyet on January 07, 2017, 12:43:50 PM Also maybe DV leak?
Title: Re: Boost leak or failed component? Post by: dokalanyi on January 09, 2017, 12:23:44 AM Also maybe DV leak? I'd come to update the thread with a solution .. Yes, the diverter valve was torn. Replaced it and the car was back to normal! |