Pages: [1] 2
Author Topic: [FIXED] rs6 load overshoot like a mofo  (Read 15154 times)
ktm733
Hero Member
*****

Karma: +18/-9
Offline Offline

Posts: 661



« on: November 06, 2016, 08:34:03 AM »

I smoke tested it and no leaks? Waste gates are set to stock breaking pressure, and it has upgraded diverter valves. It's running pig rich at wot which makes me believe I have a boost leak but I pressure tested it and boost leak tested it. These turbos are spinning way to hard, so my guess is the waste gates are not holding the pressure? I wanted to see what you guys think? I'm note trying to request 20psi either, I was shooting for around 14-17psi as youll see in the log.
« Last Edit: November 09, 2016, 02:10:28 PM by ktm733 » Logged
SB_GLI
Hero Member
*****

Karma: +116/-10
Offline Offline

Posts: 1022


« Reply #1 on: November 06, 2016, 09:54:29 AM »

log from a mostly stock rs6 shows maf readings maxing around 330 g/s while yours is 460 g/s.   The stock logs show boost higher than yours as it approaches redline.   my money is on a boost leak.

http://nefariousmotorsports.com/forum/index.php?topic=11244.0
« Last Edit: November 06, 2016, 09:56:31 AM by SB_GLI » Logged
ktm733
Hero Member
*****

Karma: +18/-9
Offline Offline

Posts: 661



« Reply #2 on: November 06, 2016, 01:04:12 PM »

I smoked the living heck out of it. Plus I pressure tested it. What would wastegate a set at the wrong cracking pressure cause? The turbos have upgraded compressor wheels
Logged
nyet
Administrator
Hero Member
*****

Karma: +608/-168
Offline Offline

Posts: 12271


WWW
« Reply #3 on: November 06, 2016, 02:19:16 PM »

Doesn't explain your rich condition or overly high load. What does ps_w look like?
Logged

ME7.1 tuning guide
ECUx Plot
ME7Sum checksum
Trim heatmap tool

Please do not ask me for tunes. I'm here to help people make their own.

Do not PM me technical questions! Please, ask all questions on the forums! Doing so will ensure the next person with the same issue gets the opportunity to learn from your ex
ktm733
Hero Member
*****

Karma: +18/-9
Offline Offline

Posts: 661



« Reply #4 on: November 06, 2016, 02:38:40 PM »

I can log it tomorrow, but what I meant by wrong cracking pressure is if they were set to low and causing to crack open under heavy boost would it cause this problem? To me it sounds possible as the turbo is trying really hard to make requested boost so duty cycle goes up and the turbos spin harder to try and make requested boost which in terms brings more air but I don't know if that air would cause the pig richness? So yes I would lean towards boost leak. When I smoke test the car it doesn't smoke at 10psi. When I pressurize (apply shop air at 15 psi) the system I think I hear a leak under the manifold but I cant tell if that's air rushing through the intake. Has anybody had any leaks under the intake manifold before? Seems rare.
Logged
ktm733
Hero Member
*****

Karma: +18/-9
Offline Offline

Posts: 661



« Reply #5 on: November 06, 2016, 02:41:50 PM »

Another weird thing.... Why am I hitting 200 load? i havent disabled any safety features or even made a load time for 200? As you can see I'm requesting 175? How is this possible, ontop of why am I not in limp mode? I dont even get a code for deviation, I get zero codes? This ecu was sent to daz to remove tuner protection and convert it for manual trans. I just don't see why I dont even get throttle cut with this big of over shoot of load.
Logged
nyet
Administrator
Hero Member
*****

Karma: +608/-168
Offline Offline

Posts: 12271


WWW
« Reply #6 on: November 06, 2016, 02:45:06 PM »

Because metered air is being lost.
Logged

ME7.1 tuning guide
ECUx Plot
ME7Sum checksum
Trim heatmap tool

Please do not ask me for tunes. I'm here to help people make their own.

Do not PM me technical questions! Please, ask all questions on the forums! Doing so will ensure the next person with the same issue gets the opportunity to learn from your ex
nubcake
Sr. Member
****

Karma: +53/-4
Offline Offline

Posts: 400


« Reply #7 on: November 06, 2016, 05:09:04 PM »

Also log MAFs separately, can help diag turbos being out of sync (or possible DV issues).
Logged
ktm733
Hero Member
*****

Karma: +18/-9
Offline Offline

Posts: 661



« Reply #8 on: November 06, 2016, 07:54:05 PM »

Also log MAFs separately, can help diag turbos being out of sync (or possible DV issues).

I did, it's right next to duty cycle. They are very close.
Logged
nubcake
Sr. Member
****

Karma: +53/-4
Offline Offline

Posts: 400


« Reply #9 on: November 07, 2016, 02:53:11 AM »

I did, it's right next to duty cycle. They are very close.

You want mshfm1/2, not msabg. Or uhfm at least.
Logged
ktm733
Hero Member
*****

Karma: +18/-9
Offline Offline

Posts: 661



« Reply #10 on: November 07, 2016, 09:43:43 AM »

You got it, almost to the shop.
Logged
ktm733
Hero Member
*****

Karma: +18/-9
Offline Offline

Posts: 661



« Reply #11 on: November 08, 2016, 04:11:44 PM »

Tested one more time, still no sign of the boost leak. Here is the log with the requested ps_w.
Logged
nyet
Administrator
Hero Member
*****

Karma: +608/-168
Offline Offline

Posts: 12271


WWW
« Reply #12 on: November 08, 2016, 04:35:38 PM »

ps_w is through the roof compared to pvdkds_w. Even worse, you've maxed it out.

You have a severe boost problem somewhere, or your MAF scaling is just plain wrong.
Logged

ME7.1 tuning guide
ECUx Plot
ME7Sum checksum
Trim heatmap tool

Please do not ask me for tunes. I'm here to help people make their own.

Do not PM me technical questions! Please, ask all questions on the forums! Doing so will ensure the next person with the same issue gets the opportunity to learn from your ex
ktm733
Hero Member
*****

Karma: +18/-9
Offline Offline

Posts: 661



« Reply #13 on: November 08, 2016, 04:58:39 PM »

I'm going to take a video to prove I don't have a boost leak. If I apply any more pressure I'm going to start blowing seals. I understand it looks like a boost leak but what else could cause this.

Backround about the car, the engine swallowed water and bent the connecting rods. So they were replaced by a profession shop. Everything has been replaced pretty much, and it's converted to manual. It has stage 2 turbos installed from a respectable company.

Is it possible a check valve could cause this?
Logged
SB_GLI
Hero Member
*****

Karma: +116/-10
Offline Offline

Posts: 1022


« Reply #14 on: November 08, 2016, 06:19:57 PM »

You can have a internal boost leak.  If you have charged air recirculating back into the intake pre turbo.  Check valves, something in PCV....
Logged
Pages: [1] 2
  Print  
 
Jump to:  

Powered by SMF 1.1.21 | SMF © 2015, Simple Machines Page created in 0.019 seconds with 16 queries. (Pretty URLs adds 0s, 0q)