Adjusted wastegate actuator until turbo pushed around 0.3-0.4 bar with N75 removed. If I go anything further, wastegate flapper becomes loose so I stopped at the last position it is still closed.
Now when N75 is back in place, pressure goes up to 0.9 bar @ WOT with stock software (should be around 0.5). I did read on here that more free flowing exhaust can cause turbo to act like that. Could this be the case or I'm still way off with adjustments?
I attached log I did today. Sadly it goes up to ~4500rpm because it was done in 3rd gear which at that point is around 100kmh and I didn't want to go any faster due to location and road condition there. But I think it is enough to see there is a problem. Can anyone with more experience take a look at it please?