zaoxdk
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« on: October 06, 2019, 01:30:17 AM »
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Hello I have had problems with not achieving the correct boost (file set to 1.1 bar) car only boosts 0.5-0.6 which is the wastegate opening pressure. The turbo which I have mounted is a K04-015. I have checked that it has the same wastegate opening pressure as on the Stock turbo. Car is a A4 B6 1.8t BFB, 518AL. When disconnecting the wastegate actuator hose from N75, it boosts fine (above 1.1 ofc). The N75 is mounted as it should, triple checked that. It’s a brand new OE unit. No boost leaks, have FMIC or restrictions in exhaust.
Has anyone experienced the same? Thanks
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fknbrkn
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mk4 1.8T AUM
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« Reply #1 on: October 06, 2019, 02:46:24 AM »
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it should push much more than 1.1 wo actuator line post logs etc
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zaoxdk
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« Reply #2 on: October 06, 2019, 03:47:43 AM »
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It does. Haven’t got any logs yet. Got it pushing at least 1.5 on the dyno W/O wastegate actuator line, but I let it off as I am on stock rods.
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zaoxdk
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« Reply #4 on: October 06, 2019, 02:36:11 PM »
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Will get some logs then. Sorry for breaking forum rulles.
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« Last Edit: October 06, 2019, 02:45:06 PM by zaoxdk »
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zaoxdk
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« Reply #5 on: October 10, 2019, 02:24:47 AM »
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Problem solved. Fitted N75 valve from a A3 8P 2.0tfsi. OE num: 06F906283F. Had to rewire the plug to a different D type connector. This valve is also much cheaper than the old style n75. Car boosts fine and holds at 1.1 as programmed.
System has been tested up to 2.5 bar - no leaks were found.
For some odd reason, the brand new OEM N75 which i had fitted must have had some problems, as it simply wouldn’t bleed enough air into the atmospheric pressure pipe.Measuring pressure at 95% n75 duty cycle at actutator connection (T pipe to a pressure gauge) resulted in 0.4-0.5 which is more than enough to open the wastegate.
Wastegate has been checked with a pressure gun, and has same opening pressure (0.5) as Stock turbo.
For any more info, please ask.
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_nameless
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« Reply #6 on: October 10, 2019, 05:11:56 AM »
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Do an output test with vcds verify its working. Did you wore it backwards? They wont work right if polarity is incorrect
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Giving your mom a tuneup
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zaoxdk
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« Reply #7 on: October 10, 2019, 06:14:39 AM »
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Yes, it is functioning as it should, dutycycle is not as High as on the Stock n75, while boost request matches boost actual. Has been wired correctly, checked polarity on diagram and valve
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