Well I did some tests today and it's not looking good.
No codes present at all.
No misfires
Smooth idle and drive
However the n75 control was the issue.
It went from 0.0% to 95%
There was no smooth tradition. Just a massive jump.
The boost would not keep up with specified.
It would boost but it was way off and it was obviously down to the issues with
controlling the n75.
Once I noticed that I stopped and pretty much placed this idea in the dead pile.
The ECU will work in a pinch if you are stuck or stranded.
but not reliable for anything other than that.
DD you are again, correct.
We should never doubt you....