K92
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« Reply #120 on: May 20, 2020, 06:59:09 AM »
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Show your dwell table or post your mod file.
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adam-
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« Reply #121 on: May 20, 2020, 07:37:46 AM »
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Set nmax to 7200, lift it well out the way. Also set KFZW/min to -30 at 7000.
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K92
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« Reply #122 on: May 20, 2020, 07:47:57 AM »
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Set nmax to 7200, lift it well out the way. Also set KFZW/min to -30 at 7000.
Meaning KFZW lowest load , first column 7000 to -30 ? Or ZWMIN maps ? Sorry have not yet stumbled on them .
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« Last Edit: May 20, 2020, 08:41:00 AM by K92 »
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K92
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« Reply #123 on: May 20, 2020, 08:44:19 AM »
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ZWMIN Oh ok, im stupid. You meant KFZWMN( did not have this map ) . All loads 7k rpm - 30 then ? Ok tested -30 . Its alot better . Is this the case, more the better ?
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« Last Edit: May 20, 2020, 10:14:57 AM by K92 »
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K92
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« Reply #124 on: May 21, 2020, 11:52:49 PM »
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adam-, it seems You know your stuff about pops and bangs. Could You please tell me why changing KFZWMN + other maps does not have effect ? I need to change KFZWMS to get the effect. As i understand KFZWMS is for engine protection. I also had to change it for hardcut limiter to -30 for kfzwmn take effect.
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« Last Edit: May 22, 2020, 01:07:00 AM by K92 »
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K92
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« Reply #125 on: May 28, 2020, 11:50:02 AM »
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So i decided to gather some logs with fixed DC-s. But boost seems weird. What could be the issue ? 1. Have tried 2 different n75 valves, result is same
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« Last Edit: May 29, 2020, 01:28:46 AM by K92 »
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adam-
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« Reply #126 on: May 29, 2020, 03:09:57 AM »
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What actuator?
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K92
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« Reply #127 on: May 29, 2020, 03:15:09 AM »
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Original garret which came with turbo . Rated 1bar actual pressure tested 0.90-0.95 Actuator seems ok, tested multiple times. I am still suspecting n75 as the oem started acting wierd, had aftermarket BS N75 on shelve but acted same.
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« Last Edit: May 29, 2020, 03:24:16 AM by K92 »
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K92
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« Reply #128 on: May 29, 2020, 09:54:34 AM »
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Same thing with new OEM N75 valve
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K92
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« Reply #129 on: May 29, 2020, 11:49:27 AM »
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Ok there is something really strange happening. Tried also direct connection from wastegate to turbo. Result is same. Tried to loosen wg, result is same, only change was boost started rising earlier? Log comparisons
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K92
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« Reply #130 on: May 29, 2020, 11:54:34 AM »
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Ok there is something really strange happening. Tried also direct connection from wastegate to turbo. Result is same. Tried to loosen wg, result is same, only change was boost started rising earlier? Actuator is moving freely when pressurised. Holds pressure Log comparisons
Sorry for quote. It was misclick Also to mention if i regulate boost with pids to 1.2-1.3 bar, then it is controllable. But i was not happy with that setup
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« Last Edit: May 29, 2020, 12:51:42 PM by K92 »
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K92
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« Reply #131 on: May 29, 2020, 12:13:52 PM »
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Yup, people have said that
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fknbrkn
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mk4 1.8T AUM
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« Reply #132 on: May 30, 2020, 01:33:26 AM »
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If you 100% sure that wg fully opened And the boost pressure higher than wg spring Then it's just a small wg hole. The Chinese crap usually comes with it
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K92
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« Reply #133 on: May 30, 2020, 02:04:15 AM »
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If you 100% sure that wg fully opened And the boost pressure higher than wg spring Then it's just a small wg hole. The Chinese crap usually comes with it
Had same tought, but its original Garret. Will detach wg from flap and test if there is full movement. If it is actuator, are there suggestions , which producer to use ? Mamba, turbosmart etc?
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K92
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« Reply #134 on: May 31, 2020, 04:29:49 AM »
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Tested today. It seems as if actuator has too small movement and it opens wg flap ~75-80%. Actuator code : A480009-6 Exhaust side : 449010-1
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