Pages: 1 ... 7 8 [9] 10 11 12
Author Topic: 2000 Audi A4 1.8T ME7.5 K04-025 need a little help with start  (Read 50164 times)
K92
Full Member
***

Karma: +0/-3
Offline Offline

Posts: 137


« Reply #120 on: May 20, 2020, 06:59:09 AM »

Show your dwell table or post your mod file.
Logged
adam-
Hero Member
*****

Karma: +122/-33
Offline Offline

Posts: 2178


« Reply #121 on: May 20, 2020, 07:37:46 AM »

Set nmax to 7200, lift it well out the way.  Also set KFZW/min to -30 at 7000.
Logged
K92
Full Member
***

Karma: +0/-3
Offline Offline

Posts: 137


« Reply #122 on: May 20, 2020, 07:47:57 AM »

Set nmax to 7200, lift it well out the way.  Also set KFZW/min to -30 at 7000.

Meaning KFZW lowest load , first column 7000 to -30 ?
Or ZWMIN maps ? Sorry have not yet stumbled on them .
« Last Edit: May 20, 2020, 08:41:00 AM by K92 » Logged
K92
Full Member
***

Karma: +0/-3
Offline Offline

Posts: 137


« Reply #123 on: May 20, 2020, 08:44:19 AM »

ZWMIN

Oh ok, im stupid. You meant KFZWMN( did not have this map ) . All loads 7k rpm - 30 then  ?
Ok tested -30 . Its alot better . Is this the case, more the better ? Cheesy
« Last Edit: May 20, 2020, 10:14:57 AM by K92 » Logged
K92
Full Member
***

Karma: +0/-3
Offline Offline

Posts: 137


« Reply #124 on: May 21, 2020, 11:52:49 PM »

adam-, it seems You know your stuff about pops and bangs. Could You please tell me why changing KFZWMN + other maps does not have effect ?  I need to change KFZWMS to get the effect.
 As i understand KFZWMS is for engine protection. I also had to change it for hardcut limiter to -30 for kfzwmn take effect.
« Last Edit: May 22, 2020, 01:07:00 AM by K92 » Logged
K92
Full Member
***

Karma: +0/-3
Offline Offline

Posts: 137


« Reply #125 on: May 28, 2020, 11:50:02 AM »

So i decided to gather some logs with fixed DC-s. But boost seems weird. What could be the issue ?
1. Have tried 2 different n75 valves, result is same
« Last Edit: May 29, 2020, 01:28:46 AM by K92 » Logged
adam-
Hero Member
*****

Karma: +122/-33
Offline Offline

Posts: 2178


« Reply #126 on: May 29, 2020, 03:09:57 AM »

What actuator?
Logged
K92
Full Member
***

Karma: +0/-3
Offline Offline

Posts: 137


« Reply #127 on: May 29, 2020, 03:15:09 AM »

Original garret which came with  turbo . Rated 1bar actual pressure tested 0.90-0.95
Actuator seems ok, tested multiple times.
I am still suspecting n75 as the oem started acting wierd, had aftermarket BS N75 on shelve but acted same.
« Last Edit: May 29, 2020, 03:24:16 AM by K92 » Logged
K92
Full Member
***

Karma: +0/-3
Offline Offline

Posts: 137


« Reply #128 on: May 29, 2020, 09:54:34 AM »

Same thing with new OEM N75 valve
Logged
K92
Full Member
***

Karma: +0/-3
Offline Offline

Posts: 137


« Reply #129 on: May 29, 2020, 11:49:27 AM »

Ok there is something really strange happening.
Tried also direct connection from wastegate to turbo. Result is same. Tried to loosen wg, result is same, only change was boost started rising earlier?
Log comparisons
Logged
K92
Full Member
***

Karma: +0/-3
Offline Offline

Posts: 137


« Reply #130 on: May 29, 2020, 11:54:34 AM »

Ok there is something really strange happening.
Tried also direct connection from wastegate to turbo. Result is same. Tried to loosen wg, result is same, only change was boost started rising earlier?
Actuator is moving freely when pressurised. Holds pressure
Log comparisons

Sorry for quote. It was misclick Also to mention if i regulate boost with pids to 1.2-1.3 bar, then it is controllable. But i was not happy with that setup
« Last Edit: May 29, 2020, 12:51:42 PM by K92 » Logged
K92
Full Member
***

Karma: +0/-3
Offline Offline

Posts: 137


« Reply #131 on: May 29, 2020, 12:13:52 PM »

Yup, people have said that
Logged
fknbrkn
Hero Member
*****

Karma: +177/-18
Offline Offline

Posts: 1401


mk4 1.8T AUM


« Reply #132 on: May 30, 2020, 01:33:26 AM »

If you 100% sure that wg fully opened
And the boost pressure higher than wg spring
Then it's just a small wg hole. The Chinese crap usually comes with it
Logged
K92
Full Member
***

Karma: +0/-3
Offline Offline

Posts: 137


« Reply #133 on: May 30, 2020, 02:04:15 AM »

If you 100% sure that wg fully opened
And the boost pressure higher than wg spring
Then it's just a small wg hole. The Chinese crap usually comes with it

Had same tought, but its original Garret. Will detach wg from flap and test if there is full movement. If it is actuator,  are there suggestions , which producer to use ? Mamba, turbosmart etc?
Logged
K92
Full Member
***

Karma: +0/-3
Offline Offline

Posts: 137


« Reply #134 on: May 31, 2020, 04:29:49 AM »

Tested today. It seems as if actuator has too small movement and it opens wg flap ~75-80%.
Actuator code : A480009-6
Exhaust side : 449010-1
Logged
Pages: 1 ... 7 8 [9] 10 11 12
  Print  
 
Jump to:  

Powered by SMF 1.1.21 | SMF © 2015, Simple Machines Page created in 0.027 seconds with 17 queries. (Pretty URLs adds 0.001s, 0q)